N44L IVPT Nearing Finish Line

Want to show off your work, or document a build? Post here.

Moderators: George Wehrung, Admin

Tom Sullivan
Posts: 80
Joined: Mon Nov 28, 2022 2:33 pm

N44L, a IVPT owned and mostly built by Joe Trepicone, is approaching the finish line. Joe is from Columbus OH and bought his kit shortly after I bought mine in 1998. About 3-4 years later we discovered each other as IVP Turbine converts, in the process of converting our kits to the Walters Turbo prop engine. The conversion was largely undocumented but pretty well supported by guys out of Deland, Florida. By networking together we were able to share our experiences with the conversion and, in a lot of ways, coming up with a better upgrade as a result.

I made many trips down to Columbus over the years, helping him close his belly tank and with wiring before his business was at a point he wanted professional help with the final wiring and instrument panel installation. My best friend Steve Phillips, was an A&P, had worked in the fielld for many years and, offered to help with that project, but only if Joe did the traveling to the U.P. He wasn’t going to live in Ohio helping him get that done.

The plane came up to our hangar July 19th, 2018, just a week before my completed IVPT went to Oshkosh for the first time. Steve, with Joe’s assistance, got a good start on the electrical and getting the instrument panel ordered. He also transported Joe’s wings to Tennessee for Brad to install his TKS panels and refit the winglets afterwards. Steve also ran the engine down to Quentin in the spring of 2019 to inspect and run, since it wasn’t one of Quentin’s engines. On Veterans Day, 2019, Steve left this world…. way too soon. I took up the commitment to help Joe get to the finish line, in spite of way too many projects on my plate already. Joe has been extremely busy as well with his Architectural Business so progress has been slower than either of us expected.

Although the plane was mostly complete, we found it was truly 90% complete, with 50% to go. A lot of that was upgrades Joe saw on mine that he wanted on his. I will try to document some of the upgrades we completed since it arrived to the U.P.

This is Post One.

Tom
Attachments
Following the driver the last mile to the airport.  He had a blast hauling it back, noting a lot of gawkers and heads turned while he was bringing it back.
Following the driver the last mile to the airport. He had a blast hauling it back, noting a lot of gawkers and heads turned while he was bringing it back.
IMG_0321.jpeg (2.28 MiB) Viewed 5337 times
IMG_0322.jpeg
IMG_0322.jpeg (2.25 MiB) Viewed 5337 times
IMG_0324.jpeg
IMG_0324.jpeg (2.62 MiB) Viewed 5337 times
IMG_0327.jpeg
IMG_0327.jpeg (3.5 MiB) Viewed 5337 times
IMG_0328.jpeg
IMG_0328.jpeg (1.58 MiB) Viewed 5337 times
Tom Sullivan
Posts: 80
Joined: Mon Nov 28, 2022 2:33 pm

One of the upgrades was modifying the tow bar with a locking mechanism to keep it from slipping off. We also built a storage system to keep the tow bar secured in the plane with a micro switch to indicate an alert if it’s not stowed during the prestart checklist.

We also fitted and bonded in the door seal.

Tom
Attachments
IMG_0423.jpeg
IMG_0423.jpeg (2.38 MiB) Viewed 5336 times
IMG_0378.jpeg
IMG_0378.jpeg (2.38 MiB) Viewed 5336 times
IMG_0365.jpeg
IMG_0365.jpeg (2.53 MiB) Viewed 5336 times
IMG_0414.jpeg
IMG_0414.jpeg (1.96 MiB) Viewed 5336 times
IMG_0381.jpeg
IMG_0381.jpeg (2.26 MiB) Viewed 5336 times
Tom Sullivan
Posts: 80
Joined: Mon Nov 28, 2022 2:33 pm

Joe decided the TKS deice system was a must so we immediately started building and installing his fluid storage tanks. They are incorporated into the floor, which he had already built the factory floor system installed so we removed that and built in the tanks.

The center area behind the console ends up being the draw tube location and the pumps and filter go right above there. We also include a drain valve in the nose wheel well so the fluid can be drained in the off season (TKS Fluid weighs nearly 9 pounds per gallon). The filler is mounted behind a small access door on the pilot side near the engine cowl. Total storage is nearly 5 gallons. I have a fluid level induction system as well.

Tom
Attachments
IMG_4267.jpeg
IMG_4267.jpeg (2.22 MiB) Viewed 5336 times
IMG_4268.jpeg
IMG_4268.jpeg (2.23 MiB) Viewed 5336 times
IMG_4352.jpeg
IMG_4352.jpeg (2.12 MiB) Viewed 5336 times
IMG_4529.jpeg
IMG_4529.jpeg (2.22 MiB) Viewed 5336 times
IMG_4353.jpeg
IMG_4353.jpeg (2.03 MiB) Viewed 5336 times
IMG_4356.jpeg
IMG_4356.jpeg (1.15 MiB) Viewed 5336 times
Tom Sullivan
Posts: 80
Joined: Mon Nov 28, 2022 2:33 pm

More pictures of the TKS Filler point and door. Like the actual fluid tanks, the filler bucket was eventually sealed with fuel tank sealer. The door received a primer coat when all other areas needing primer were sprayed.
Attachments
IMG_4716.jpeg
IMG_4716.jpeg (1.21 MiB) Viewed 5334 times
IMG_4707.jpeg
IMG_4707.jpeg (1.1 MiB) Viewed 5334 times
Actual cap covered with blue tape.  This is the bucket built for the filler neck and cap, with a recess for the rudder bell crank to swing without hitting the bucket.
Actual cap covered with blue tape. This is the bucket built for the filler neck and cap, with a recess for the rudder bell crank to swing without hitting the bucket.
IMG_4515.jpeg (1.32 MiB) Viewed 5334 times
Tom Sullivan
Posts: 80
Joined: Mon Nov 28, 2022 2:33 pm

Other TKS work required. We installed the TKS panels on the Horizontal Stabilizer. Not fun working upside down for the bottom side work. We set up saw horses and large blankets allowing us to work while laying on our backs. Proved to be a great idea for old farts taking on young men’s work!

I had a spray bar welded up by a local stainless steel welding guru and sent out for “EDM” machined .014” holes at 1” spacing across the tube. The wind deflector was laid up over a Styrofoam mold, body worked and primed.

I added a few pictures of my special A/C drive with auto belt tensioning system. The drive was designed by me, machined by a Menonite in Central Wisconsin, and has worked flawlessly on my own IVPT driving a 16,000 BTU A/C system.
Attachments
IMG_2753.jpeg
IMG_2753.jpeg (2.3 MiB) Viewed 5334 times
IMG_2754.jpeg
IMG_2754.jpeg (2.13 MiB) Viewed 5334 times
IMG_6019.jpeg
IMG_6019.jpeg (1.77 MiB) Viewed 5334 times
IMG_4554.jpeg
IMG_4554.jpeg (2.09 MiB) Viewed 5334 times
IMG_4555.jpeg
IMG_4555.jpeg (1.97 MiB) Viewed 5334 times
IMG_4687.jpeg
IMG_4687.jpeg (2.1 MiB) Viewed 5334 times
Last edited by Tom Sullivan on Sun May 12, 2024 1:32 pm, edited 1 time in total.
Tom Sullivan
Posts: 80
Joined: Mon Nov 28, 2022 2:33 pm

A few more TKS pictures from installing on the HS.

I added the beautiful bracket built by Garth for the brushes on the prop for prop heat. A ton cheaper than Avia.
Attachments
IMG_5852.jpeg
IMG_5852.jpeg (2.28 MiB) Viewed 5334 times
IMG_5842.jpeg
IMG_5842.jpeg (1.97 MiB) Viewed 5334 times
IMG_5975.jpeg
IMG_5975.jpeg (1.32 MiB) Viewed 5334 times
IMG_5842.jpeg
IMG_5842.jpeg (1.97 MiB) Viewed 5334 times
Tom Sullivan
Posts: 80
Joined: Mon Nov 28, 2022 2:33 pm

Joe had lost his interior panels, made out of carbon fiber. He bought some Divinycel (core) and we laid up all his new panels with one layer of CF on each side, then vacuum bagged them. They turned out AWESOME! Very light yet stronger than the original Lancair ones made with fiberglass.

We installed the upper closeout aft pressure bulkhead and then his A/C evaporator / fan assembly. It is a hot rod conversion unit and 12 volt so he installed a nice size voltage converter. His inlet air to cool his condenser is routed from the aft NACA Duct in his vertical tail, with a servo controlled scoop on the exit. That was wired initially by an Airbus tech from Europe, but was extremely complicated with multiple relays and circuit boards, with no wiring diagrams. We de-complicated the system with new simple relays.

His baggage tank was installed for extra fuel capacity. He will have well over 5 hours of fuel range.
Attachments
Vacuum bagged interior panel.
Vacuum bagged interior panel.
IMG_6143.jpeg (1.23 MiB) Viewed 5330 times
IMG_6024.jpeg
IMG_6024.jpeg (1.96 MiB) Viewed 5330 times
A/C Evaporator- Fan assembly installed on upper aft pressure bulkhead.  Note the condensate drain for water running under the unit through the bulkhead.
A/C Evaporator- Fan assembly installed on upper aft pressure bulkhead. Note the condensate drain for water running under the unit through the bulkhead.
IMG_5796.jpeg (1.67 MiB) Viewed 5330 times
IMG_4737.jpeg
IMG_4737.jpeg (2.09 MiB) Viewed 5330 times
IMG_4736.jpeg
IMG_4736.jpeg (1.91 MiB) Viewed 5330 times
Fuel filler for the baggage fuel tank.  Also note the condensate drain line for the A/C coming through the pressure bulkhead with the hose running to a special drain valve (home made) that only allows drainage when water is present, otherwise sealing for cabin pressurization.
Fuel filler for the baggage fuel tank. Also note the condensate drain line for the A/C coming through the pressure bulkhead with the hose running to a special drain valve (home made) that only allows drainage when water is present, otherwise sealing for cabin pressurization.
IMG_5797.jpeg (1.83 MiB) Viewed 5330 times
Belly tank before installation
Belly tank before installation
IMG_5837.jpeg (1.7 MiB) Viewed 5330 times
Tom Sullivan
Posts: 80
Joined: Mon Nov 28, 2022 2:33 pm

Joe asked me to check his engine angles because I had a much more precise method (with lasers and electronic angle meters) of locking in the angles. My plane was a true 300 knot airframe, while most are in the 270 - 280 knot range. Although many other speed mods had been incorporated in mine (of which most were also added to his) I believe this setup to be one of the most critical.

After resetting his engine angles, we found some misalignment we needed to address of his cowls and intake system. Another of my speed mods (noted by both Quentin and Brad) was my overlap flanges on the front of the intake transitions to the intake scoops, sealed with a specially designed rubber “strap clamp”.. We use the Chris Scoppe intake system which is clearly superior in efficiency to other systems, but now with a virtually sealed connection. It also “locates” the lower cowl firmly in the same place during every installation. The ram air effect of intake air via this intake system is evident in cruise speeds.
Attachments
Extending and mating the intake transition for perfect fit to the intake scoop
Extending and mating the intake transition for perfect fit to the intake scoop
IMG_6357.jpeg (1.28 MiB) Viewed 5327 times
The fit of my intake shown that we were trying to repeat on Joe’s plane. Note the rubber clamp seal slid back on the transition that seals the joint once everything is assembled
The fit of my intake shown that we were trying to repeat on Joe’s plane. Note the rubber clamp seal slid back on the transition that seals the joint once everything is assembled
IMG_6355.jpeg (1.16 MiB) Viewed 5327 times
Overlap flange newly added and shown from inside the intake scoop
Overlap flange newly added and shown from inside the intake scoop
IMG_6380.jpeg (1.34 MiB) Viewed 5327 times
Overlap flange shown from the top of the intake scoop / transition joint
Overlap flange shown from the top of the intake scoop / transition joint
IMG_6381.jpeg (1.94 MiB) Viewed 5327 times
Micro applied inside the intake transition
Micro applied inside the intake transition
IMG_7687.jpeg (1.26 MiB) Viewed 5327 times
IMG_0070.jpeg
IMG_0070.jpeg (3.02 MiB) Viewed 5327 times
IMG_0076.jpeg
IMG_0076.jpeg (4.12 MiB) Viewed 5327 times
IMG_0077.jpeg
IMG_0077.jpeg (3.86 MiB) Viewed 5327 times
Final prop to cowl alignment
Final prop to cowl alignment
IMG_0072.jpeg (3.5 MiB) Viewed 5327 times
Tom Sullivan
Posts: 80
Joined: Mon Nov 28, 2022 2:33 pm

More cowling and intake plenum work.

The top several pictures are his intake plenum and modified intake transitions after an amazing clear coat finish.

The Skoppe top cowl had an update after the first couple kit deliveries, namely a stiffener added at the top aft area to give the cowl rigidity. Joe’s turbine conversion kit was an early one without the stiffener. Mine had the stiffener but needed modifying because it was too narrow at the aft flanges. We prepped and cleaned Joe’s top cowl, fitted foam for the stiffener, and overlaid carbon fiber on it. We installed peel ply and then installed the cowl so the curvature of the stiffened cowl exactly matched the final installation fit.

Another issue of this otherwise great cowling was the sides along the seam, at 300 knots, would get pushed in enough on mine that the cowl fastener back area would rub on the intake plenum, creating damage almost immediately. I designed a stiffener out of 1/8” x 1” aluminum strap on edge, radiused in a vice to the exact curvature of the cowl for each side, attached with epoxy and then reinforced with 4 bids of CF. Result, the lower cowl seam to the upper cowl gains a ton more strength with no deformation under 300 knot wind loads.
Attachments
Intake transition to intake scoop rubber clamp seal
Intake transition to intake scoop rubber clamp seal
IMG_0608.jpeg (3.1 MiB) Viewed 5322 times
Top cowl prepped with foam for CF stiffener.
Top cowl prepped with foam for CF stiffener.
IMG_0103.jpeg (3.45 MiB) Viewed 5322 times
Upper plenum close out with fresh clear coat
Upper plenum close out with fresh clear coat
IMG_0231.jpeg (3.17 MiB) Viewed 5322 times
Intake transitions with overlap flange mods, lower plenum close outs, and a new dual battery box in fresh clear coat.
Intake transitions with overlap flange mods, lower plenum close outs, and a new dual battery box in fresh clear coat.
IMG_0232.jpeg (3.23 MiB) Viewed 5322 times
Plenum parts installed
Plenum parts installed
IMG_0235.jpeg (3.91 MiB) Viewed 5322 times
IMG_0236.jpeg
IMG_0236.jpeg (3.6 MiB) Viewed 5322 times
CF installed on top cowl stiffener before installation on plane for curing in proper curve of cowl
CF installed on top cowl stiffener before installation on plane for curing in proper curve of cowl
IMG_0104.jpeg (4.19 MiB) Viewed 5322 times
Initial installment of aluminum stiffeners
Initial installment of aluminum stiffeners
IMG_7651.jpeg (1.65 MiB) Viewed 5322 times
CF installed on aluminum cowl seam stiffeners
CF installed on aluminum cowl seam stiffeners
IMG_7654.jpeg (1.45 MiB) Viewed 5322 times
IMG_7653.jpeg
IMG_7653.jpeg (1.45 MiB) Viewed 5322 times
Tom Sullivan
Posts: 80
Joined: Mon Nov 28, 2022 2:33 pm

A few more cowling repair pictures and a bump out for A/C controls in the overhead.
Attachments
I had to form a “bump out” for clearance for the A/C controls in the overhead. I wondered if it was formed nice enough to clear coat instead of bodywork and painting it?  We included it with some other clear coat items later and it looks great.
I had to form a “bump out” for clearance for the A/C controls in the overhead. I wondered if it was formed nice enough to clear coat instead of bodywork and painting it? We included it with some other clear coat items later and it looks great.
IMG_0664.jpeg (3.68 MiB) Viewed 5322 times
IMG_0234.jpeg
IMG_0234.jpeg (3.45 MiB) Viewed 5322 times
IMG_0233.jpeg
IMG_0233.jpeg (3.1 MiB) Viewed 5322 times
IMG_0105.jpeg
IMG_0105.jpeg (3.7 MiB) Viewed 5322 times
IMG_0080.jpeg
IMG_0080.jpeg (3.61 MiB) Viewed 5322 times
IMG_0079.jpeg
IMG_0079.jpeg (3.35 MiB) Viewed 5322 times
Post Reply